›› 2018, Vol. 39 ›› Issue (3): 863-871.doi: 10.16285/j.rsm.2016.0600

• 基础理论与实验研究 • 上一篇    下一篇

粉质黏土填料在K30试验加载进程中的变形时间效应状态分析

熊 勇1, 2,罗 强1, 2,张 良1, 2,蒋良潍1, 2,朱江江1, 2   

  1. 1. 西南交通大学 土木工程学院,四川 成都 610031;2. 西南交通大学 高速铁路线路工程教育部重点实验室,四川 成都 610031
  • 收稿日期:2016-03-28 出版日期:2018-03-12 发布日期:2018-06-06
  • 通讯作者: 罗强,男,1963年生,博士,博士生导师,主要从事路基与土工技术方面的研究工作。E-mail: LQrock@home.swjtu.edu.cn E-mail:yongx1118@163.com
  • 作者简介:熊勇,男,1987年生,博士研究生,主要从事铁路路基方面的研究工作。
  • 基金资助:

    重点基础研究发展计划(973)项目(No.2013CB036204);国家自然科学基金青年基金项目(No.51408491)。

Analysis of deformation time effect of silt clay filler in K30 loading process

XIONG Yong1, 2, LUO Qiang1, 2, ZHANG Liang1, 2, JIANG Liang-wei1, 2, ZHU Jiang-jiang1, 2   

  1. 1. School of Civil Engineering, Southwest Jiaotong University, Chengdu, Sichuan 610031, China; 2. MOE Key Laboratory of High-speed Railway Engineering, Southwest Jiaotong University, Chengdu, Sichuan 610031, China
  • Received:2016-03-28 Online:2018-03-12 Published:2018-06-06
  • Supported by:

    This work was supported by the National Program on Key Basic Research Project of China (973 Program) (2013CB036204) and the National Natural Science Fund Youth Fund Project (51408491).

摘要: 变形稳定标准和分级加载制度是影响K30试验效率和准确性的关键因素,与加载进程中填土的变形时间效应状态密切相关。开展了3组最优含水率下压实系数K分别为0.90、0.95和1.00填土模型的小型平板载荷试验,获得了不同荷载作用下填土变形时程曲线和弹塑性变形数据,讨论了在K30试验加载进程中填土变形状态的变化及其对加载稳定时间的影响。试验表明:良好压实的粉质黏土填料,在K30试验进程中的变形以弹性为主,处于缓慢收敛状态,随着加载级数增加,塑性变形比例逐渐增大,变形时间效应呈现出由微弱进入明显状态的演化趋势,变形1.25 mm对应于缓慢收敛中的微弱时间效应亚状态;“变形速率不超过0.01 mm/min”变形稳定标准分级加载时间随时间效应指数呈加速增长规律,能在保证试验精度的基础上提高试验效率;以最大荷载下填土变形时间效应不应超过显著状态、变形量不小于1.25 mm为约束条件,针对5级加载、0.04 MPa荷载增量的加载制度,可得K30试验的适宜范围为60~160 MPa/m。

关键词: 铁路路基, 粉质黏土, K30试验, 时间效应, 变形状态

Abstract: The standard of deformation stability and the design of stepwise loading are the key factors affecting the efficiency and accuracy of K30 test, and closely related to deformation time-effect state of the filling in the loading process. To get time history curve and deformation data, three small plate loading tests of unit structure filling models are carried out in optimal water rate at compaction coefficient (K) of 0.90, 0.95 and 1.00. The change of the deformation state of the soil during the loading process of K30 test and the influence of the loading stability time are discussed. The results indicate that, the deformation of well compacted silty clay filler in the process of K30 test is mainly elastic, and almost in state of slow convergence. With the increasing of load, the ratio of plastic deformation gradually develops, and the evolution trend of deformation state is presented from weak to strong. When accumulated to 1.25 mm, the deformation is in the sub-state of weak in slow convergence. The standard of “0.01 mm/min”, step-loading time of which shows accelerating growth pattern, can apparently reduce test time with acceptable test error. On the principle that the deformation state should be in apparent state during loading process, and deformation should exceed 1.25 mm, for loading system of five steps and 0.04 MPa load increment, it is suggested that the K30 value in the detection of compaction quality of fine grained soil filler should be between 60-160 MPa/m.

Key words: railway subgrade, silt clay, K30 test, time effect, deformation state

中图分类号: 

  • TU 411

[1] 杨艳霜, 周辉, 梅松华, 张占荣, 李金兰. 高地应力硬脆性围岩开挖损伤区时效性扩展案例分析——特征与机制[J]. 岩土力学, 2020, 41(4): 1357-1365.
[2] 刘建民, 邱月, 郭婷婷, 宋文智, 谷川, . 饱和粉质黏土静剪强度与振动后 静剪强度对比研究[J]. 岩土力学, 2020, 41(3): 773-780.
[3] 王青元, 刘杰, 王培涛, 刘飞, . 冲击扰动诱发蠕变岩石加速失稳破坏试验[J]. 岩土力学, 2020, 41(3): 781-788.
[4] 刘家顺, 王来贵, 张向东, 李学彬, 张建俊, 任 昆, . 部分排水时饱和粉质黏土变围压循环三轴试验研究[J]. 岩土力学, 2019, 40(4): 1413-1419.
[5] 胡田飞, 刘建坤, 王天亮, 岳祖润, . 粉质黏土变形特性的冻融循环效应及其双屈 服面本构模型[J]. 岩土力学, 2019, 40(3): 987-997.
[6] 丁瑜, 陈晓斌, 张家生, 贾羽, . 风化红砂岩残积土路基瞬态饱和区动态水压力 特征试验研究[J]. 岩土力学, 2019, 40(12): 4740-4750.
[7] 杨文保, 吴琪, 陈国兴, . 长江入海口原状土动剪切模量预测方法探究[J]. 岩土力学, 2019, 40(10): 3889-3896.
[8] 刘家顺,张向东,孙嘉宝,杨建军,方天健. 主应力轴旋转下K0固结饱和粉质黏土孔压及变形特性试验研究[J]. , 2018, 39(8): 2787-2794.
[9] 许宏发,柏 准,齐亮亮,耿汉生,马林建,刘 斌, . 基于全应力-应变曲线的软岩蠕变寿命估计[J]. , 2018, 39(6): 1973-1980.
[10] 刘松玉,曹菁菁,蔡光华, . 活性氧化镁碳化固化粉质黏土微观机制[J]. , 2018, 39(5): 1543-1552.
[11] 李连祥,符庆宏,黄佳佳, . 砂土地基和粉质黏土地基基坑悬臂开挖离心模型试验[J]. , 2018, 39(2): 529-536.
[12] 陈树峰,孔令伟,黎澄生, . 低幅应变条件下粉质黏土泊松比的非线性特征[J]. , 2018, 39(2): 580-588.
[13] 裴书锋,冯夏庭,张建聪,王鹏飞,江 权,周扬一,郝宪杰,刘俊峰,. 高边坡坝基柱状节理玄武岩开挖卸荷时效松弛特性[J]. , 2018, 39(10): 3743-3754.
[14] 杨光昌,白 冰. 考虑超固结效应的不同温度路径下饱和粉质黏土的热固结[J]. , 2018, 39(1): 71-77.
[15] 李术才,陈红宾,章 冲,龚英杰,李会良,丁万涛,王 琦,. 粉质黏土隧道超前支护作用效果研究[J]. , 2017, 38(S2): 287-294.
Viewed
Full text


Abstract

Cited

  Shared   
  Discussed   
No Suggested Reading articles found!