岩土力学 ›› 2018, Vol. 39 ›› Issue (S2): 231-237.doi: 10.16285/j.rsm.2018.1528

• 基础理论与实验研究 • 上一篇    下一篇

片理化玄武岩隧道围岩大变形控制现场试验研究

崔光耀1,祁家所1,王明胜2   

  1. 1. 北方工业大学 土木工程学院,北京 100144;2. 中国中铁隧道集团有限公司,广东 广州 511458
  • 收稿日期:2018-08-18 出版日期:2018-12-21 发布日期:2019-01-04
  • 作者简介:崔光耀,男,1983年生,博士,副教授,主要从事隧道与地下工程的教学与研究
  • 基金资助:
    国家自然科学基金项目(No.51408008);北京市青年拔尖人才培育计划项目(No.1816008);中铁隧道集团科技创新计划项目(No.548418K5)。

Field test study on large deformation control of surrounding rock of cleaved basalt tunnel

CUI Guang-yao1, QI Jia-suo1, WANG Ming-sheng2   

  1. 1. College of Architecture and civil Engineering, North China University of Technology, Beijing, 100144, China; 2. China Railway Tunnel Group Co., Ltd., Guangzhou, Guangdong 511458, China
  • Received:2018-08-18 Online:2018-12-21 Published:2019-01-04
  • Supported by:
    This work was supported by the National Science Foundation of China(51408008), Foundation for Youth Talent Training Plan of Beijing(1816008), and Foundation for Science and Technology Innovation Project of CTG(548418K5).

摘要: 丽香中义隧道片理化玄武岩段地质构造复杂,围岩软弱、破碎,地下水较发育,地应力极高,边墙大变形灾害突出,开展了3种围岩大变形施工控制技术措施的现场试验研究。现场试验结果表明,从支护加强角度出发的大变形Ⅰ型支护方案和大变形Ⅱ型支护方案,试验段边墙变形得到了较好的控制,换拱率由100%分别降至38.50%和22.22%;开挖断面支护成环时间对边墙收敛变形控制影响巨大,掌子面开挖后断面支护应尽快封闭成环;从支护和围岩双向加强角度出发的“大变形Ⅱ型支护+边墙施设6.5 m长锚杆”施工方案,成功控制了试验段边墙的大变形灾害,换拱率降至0%。研究成果可为类似工程提供参考。

关键词: 片理化玄武岩, 高地应力, 围岩大变形, 现场试验

Abstract: The geological structure of cleaved basalt section of Zhongyi tunnel of Lixiang Railway is complex; the surrounding rock is weak and broken; the groundwater is well developed; the ground stress is extremely high; and the side wall deformation disaster is prominent; therefor three field test researches on construction control measures for large deformation of surrounding rock have been carried out. The field test results show that: From the perspective of support reinforcement, working condition 1 and working condition 2, the deformation of the side wall of the test section has been well controlled; and the arch changing rate decreased from 100% to 38.50% and 22.22% respectively; the ringing time of the excavation section has a great influence on the control of side wall convergence and deformation; the section support after excavation of the tunnel face should be closed as soon as possible; the perspective of support and surrounding rock two-way reinforcement of the working condition 3 of “large deformation type II support + side wall with 6.5 m long anchor rod” is adopted to successfully control the large deformation disaster of the test section side wall and the arch changing rate drops to 0%. The research results can provide reference for similar projects.

Key words: cleaved basalt, high geostress, surrounding rock large deformation, field test

中图分类号: 

  • TU452
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